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  1. Data Management
  2. DM-29792

Camera Hexapod: The Enabled substate needs to be changed "manually" to "clearError" caused by unplugging the motor power cable.

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    Details

      Description

      After unplugging and re-plugging the motor power cable:
       
      Step
      Send the "clearError" trigger and bring the system to the Enabled/Stationary state.
       
      Expected Result
      The system is in the Enabled/Stationary state and ready to be commanded.
       
      Actual Result
      Fault cleared, the system is in StandbyState.
      Transitioned to enabled trough EUI
      Entered into Enabled/MovingPT-PT without hexapod movement.
      Stop command send through EUI.
      Status changed to enabled /stationary.

      Moved back to zero successfully.

        Attachments

          Activity

          hdrass Holger Drass created issue -
          hdrass Holger Drass made changes -
          Field Original Value New Value
          Assignee Bo Xin [ bxin ] Andy Clements [ aclements ]
          aclements Andy Clements made changes -
          Assignee Andy Clements [ aclements ] Te-Wei Tsai [ ttsai ]
          ttsai Te-Wei Tsai made changes -
          Epic Link DM-27621 [ 441885 ]
          ttsai Te-Wei Tsai made changes -
          Component/s ts_main_telescope [ 16710 ]
          hdrass Holger Drass made changes -
          Link This issue relates to SUMMIT-5251 [ SUMMIT-5251 ]
          hdrass Holger Drass made changes -
          Link This issue relates to SUMMIT-5404 [ SUMMIT-5404 ]
          hdrass Holger Drass made changes -
          Description After unplugging and re-plugging the motor power cable:
           
          *Step*
          Send the "clearError" trigger and bring the system to the Enabled/Stationary state.
           
          *Expected Result*
          The system is in the Enabled/Stationary state and ready to be commanded.
           
          *Actual Result*
          Fault cleared, the system is in StandbyState.
          Transitioned to enabled trough EUI
          Entered into Enabled/MoivingPT-PT without hexapod movement.
          Stop command send through EUI.
          Status changed to enabled /stationary.

          Moved back to zero successfully.
          After unplugging and re-plugging the motor power cable:
            
           *Step*
           Send the "clearError" trigger and bring the system to the Enabled/Stationary state.
            
           *Expected Result*
           The system is in the Enabled/Stationary state and ready to be commanded.
            
           *Actual Result*
           Fault cleared, the system is in StandbyState.
           Transitioned to enabled trough EUI
           Entered into Enabled/MovingPT-PT without hexapod movement.
           Stop command send through EUI.
           Status changed to enabled /stationary.

          Moved back to zero successfully.
          aclements Andy Clements made changes -
          Epic Link DM-27621 [ 441885 ]
          ttsai Te-Wei Tsai made changes -
          Epic Link DM-32113 [ 770361 ]
          Watchers Andy Clements, Bo Xin, Holger Drass [ Andy Clements, Bo Xin, Holger Drass ] Andy Clements, Holger Drass [ Andy Clements, Holger Drass ]
          ttsai Te-Wei Tsai made changes -
          Epic Link DM-32113 [ 770361 ] DM-27623 [ 441888 ]
          hdrass Holger Drass made changes -
          Link This issue relates to SUMMIT-5796 [ SUMMIT-5796 ]
          aclements Andy Clements made changes -
          Epic Link DM-27623 [ 441888 ] DM-27622 [ 441886 ]
          aclements Andy Clements made changes -
          Epic Link DM-27622 [ 441886 ] DM-27721 [ 442128 ]

            People

            Assignee:
            ttsai Te-Wei Tsai
            Reporter:
            hdrass Holger Drass
            Watchers:
            Andy Clements, Holger Drass
            Votes:
            0 Vote for this issue
            Watchers:
            2 Start watching this issue

              Dates

              Created:
              Updated:

                Jenkins

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