Details
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Type:
Story
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Status: Done
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Resolution: Done
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Fix Version/s: None
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Component/s: ts_main_telescope
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Labels:
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Story Points:0
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Sprint:TSSW Sprint - Nov 07 - Nov 21
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Team:Telescope and Site
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Urgent?:No
Description
Check the possibility to bypass the linear encoder fault in rotator controller. This is related to FRACAS-130. The log file is 2022_11_17_22_48_04.log
Attachments
Issue Links
- relates to
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DM-35339 Support the Rotator Test on Summit Part 7
- Done
Activity
Field | Original Value | New Value |
---|---|---|
Link | This issue is triggered by SUMMIT-6947 [ SUMMIT-6947 ] |
Summary | Check the Possibility to Bypass the Linear Encoder Fault in Rotator | Check the Possibility to Bypass the Linear Encoder Fault in Rotator Controller |
Description | Check the possibility to bypass the linear encoder fault in rotator. | Check the possibility to bypass the linear encoder fault in rotator controller. |
Description | Check the possibility to bypass the linear encoder fault in rotator controller. | Check the possibility to bypass the linear encoder fault in rotator controller. This is related to FRACAS-130. |
Attachment | 2022_11_17_22_48_04.log [ 64739 ] |
Description | Check the possibility to bypass the linear encoder fault in rotator controller. This is related to FRACAS-130. | Check the possibility to bypass the linear encoder fault in rotator controller. This is related to FRACAS-130. The log file is [^2022_11_17_22_48_04.log] |
Sprint | TSSW Sprint - Nov 21 - Dec 05 [ 1201 ] | TSSW Sprint - Nov 07 - Nov 21 [ 1200 ] |
Status | To Do [ 10001 ] | In Progress [ 3 ] |
Attachment | data_rotator.mat [ 64744 ] |
Attachment | stickyEventStatus.png [ 64746 ] |
Attachment | feedbackError.png [ 64747 ] |
Attachment | linearEncoderFault.jpg [ 64748 ] |
Attachment | LinearEncoder1Fault.jpg [ 64749 ] |
Attachment | motorEncoder1.jpg [ 64750 ] |
Attachment | linearEncoder1_10192022.jpg [ 64751 ] |
Story Points | 0 |
Watchers | Te-Wei Tsai [ Te-Wei Tsai ] | Bruno Quint, Felipe Daruich, Te-Wei Tsai [ Bruno Quint, Felipe Daruich, Te-Wei Tsai ] |
Reviewers | Bruno Quint [ bquint ] | |
Status | In Progress [ 3 ] | In Review [ 10004 ] |
Status | In Review [ 10004 ] | Reviewed [ 10101 ] |
Resolution | Done [ 10000 ] | |
Status | Reviewed [ 10101 ] | Done [ 10002 ] |
Reformat the data to mat file for the analysis: data_rotator.mat
Linear Encoder Fault:
Linear Encode 1 Value:
We can see the significant fluctuation. This happens for the linear encoder 2 as well.
Compared with this, the motor encoder 1 and 2 looks smooth:
Compared with the above data, I have a data at 10/19/2022 (
DM-35339) that shows the linear encoder data should be smooth: